#Motor fail
67 messages · Page 1 of 1 (latest)
I tried to get it to take off in my garden and it started getting higher and higher and vibrating. Isn't that what caused the problem?
At first I tried more freestyle PIDs but I saw the reaction of the drone so I put back the basic ones but the drone still reacted in the same way by vibrating and climbing
you mean you applied a preset?
No, I looked on sites to adjust a 3 inch in freestyle but it failed.
And now they do this
the drone will not behave normally without props, the motors spinning up under these conditions is expected behaviour
this is a bind and fly right?
load the cli from the manufacturer to get it back to defaults and you should be good
Yes
it should have been decently tuned from factory, unless you know what you are doing then i wouldn't try to mess with it
Where i can find this ?
For the cli ?
this is the oasis fly 30 right?
they actually dont have the cli dump listed as far as i can see
if thats true that pretty shitty of them
Yeah i don't see the cli :/
That is
i guess contact sub 250 and ask for the cli
i do that right now
I think i see the CLI and now what i need to do ? https://sub250.com/apps/help-center#hc-oasisfly30-25-o4-cli
Welcome to Sub250 drone store. Sub250 strives to create durable, reliable, and high-performance mini RC racing drones & micro-quads for our customers at the best price. You can find under 250g Micro FPV drones & Quadcopters with parts, FPV goggles, FPV cameras, flight controllers from this fpv drone kit online store.
i copy / past that ? ''
go to the cli tab and press load from file
pick the file and press execute
if it doesn't reboot automatically write save and press enter and it should reboot
and u think all problem is gone with this ?
unless you broke somthing physicaly it should be gone once you load the cli and set up the quad again
Hello, i do the CLI restore and my drone allways do a fail (vidéo) they vibrating
i make a video for show all my setup on beta fligth and the reaction of the drone
After having done a pleasant but slow flight session for the backflips and rolls I wanted to increase the PID and rate of the drone (I had never opened beta flight before, and it is my first real FPV) and my drone reacts in a strange way vibrations, uncontrollable, I cannot find the solution, when I copy and paste the CLI of the drone given by e...
@raven hearth was this the same flyaway thing yours did when the board orientation was wrong?
Its freaked out
?
@slow oriole check that the drone moves correctly in the setup tab when you move it in real life
if its off by like 45 degrees when you pitch and roll the copter then its a problem
There's actually a problem with this when I tilt the drone forward in real life, it tilts diagonally backward to the left. In the software, how should I fix this?
Thank you very much for taking the time to troubleshoot my problem 🙂
board orientation on the configuration tab
When I tilt the drone forward it looks like this on the software how I fix it 🙂
@slow oriole
I'm in it but I can't get it to lean forward on the software
Ok i do this (screen) and now they work good on software u think all my problem is gone ? i can try to fly, with no problem ?
looked like you onyl needed an 0ffset of 45 degrees
it went forward and left when you went forward
Only 45 on YAW?
The last flight the drone was backward left when I was moving forward, I won't allow myself to test it until it's good x)
45 degrees in YAW is not working 225 still working is a problem to stay with 225 in YAW ?
use whatever is correct in the setup tab
I just went to do a test, everything worked perfectly, I thank you very much for all your help, but I had another problem, I tried to make the drone beep after a crash and nothing to do the bind is not set or I don't know what but it did not want to beep do you know what I can do for that?
if you want the motors to beep make sure that rx_set is turned on under dshot configuration in the configuration tab. additionally make sure that the switch for the beeper is set up in the modes tab
Thank you so much man, you boosted me in the world of fpv I knew how to set the mode alone to turn around after a crash two days ago I would never have been able to, you taught me a lot man, thanks again 🙂 ♡