Hi guys,
I'm running the mentioned FC on my racing build, and I'm experiencing an issue:
Randomly, the quad makes an aggressive turn so that it becomes uncontrollable for a short period of time, as you can see in the video.
I assume that the problem is caused by a bad gyro? What do you guys think?
The build is very clean and there is no cable on top of the FC.
Hardware:
Frame: DinDrones Southeast Typhon V7 T700 - 5"
Esc: Foxeer Reaper F4 Slim Mini 60a
FC: Mamba F722 Mini MK4 MPU6000
Props: HQProp R38
Lipo: Bonka 1380 6s 150C
Motors: Xnovamotors LiteSpeed 2050kv
Thanks for your help!
Fabian