#Eva3 + beacon problem

15 messages · Page 1 of 1 (latest)

broken jay
#

hi,

my configuration
Ratrig-300
EVA3 Phaetus Rapido HF
Orbiter 2.0
Octopus 1.1
Toolboard EBB42-12

I have upgrade my Ratrig 300 with a Beacon sensor.
BEACON_CALIBRATE is done.

my problem:

  1. BED MESH stop working
  2. unable to BED_MESH_CALIBRATE

if variable_calibrate_bed_mesh=False, I'm able to print but without BEDMESH
variable_adaptive_mesh=False

error report:
Move out of range: 20.000 -7.000 2.000 [0.000]

seem Y is out of range (ini variable missing ?)

printer.cfg
https://pastebin.com/raw/Hw14cMu1

klippy.log
https://pastebin.com/raw/SC7MTAs9

any idea how to fix this ?

fossil pulsar
fast elk
#

[beacon]
serial: /dev/serial/by-id/usb-Beacon_Beacon_RevD_B5BAC37A4E4B333448202020FF0A0E36-if00
x_offset: 0
y_offset: 27
mesh_main_direction: x
mesh_runs: 2
speed: 15.
lift_speed: 80.

[stepper_z]
homing_retract_dist: 0
endstop_pin: probe:z_virtual_endstop

[safe_z_home]
home_xy_position: 100, 100 # update for your machine

z_hop: 3

#

out of my printer.cfg without using silly includes for a 200

#

[z_tilt]
z_positions:
0,0
100,200
200,0

points:
10,10
100,160
190,10

horizontal_move_z: 12
retries: 10
retry_tolerance: 0.01
speed: 500

#

And make sure the middle point in the back is 40 away from the bed border

#

lol, just saw on my github that the includes are acitvated. Must have missed it. The moment I have that thing online I will check what is in there and if it is really needed.

broken jay
#

hi,

#

[include RatOS/printers/v-core-3/300.cfg]
[stepper_x]
position_max: 300
position_endstop: 0

[stepper_y]
position_max: 300
position_endstop: 300

[stepper_z]
position_max: 300

[bed_mesh]
horizontal_move_z: 5
mesh_min: 20,20
mesh_max:265,260
probe_count: 7,7
fade_start: 1.0
fade_end: 10.0
mesh_pps: 2,2
algorithm: bicubic
bicubic_tension: .2

[z_tilt]
z_positions:
0,0
150,300
300,0

points:
60,60
185,270
260,60

horizontal_move_z: 20
retries: 10
retry_tolerance: 0.02

[include RatOS/z-probe/beacon.cfg]
[beacon]
serial: /dev/beacon
x_offset: 0
y_offset: 27
mesh_main_direction: x
mesh_runs: 2
speed: 15.
lift_speed: 80.

[stepper_z]
homing_retract_dist: 0

#

from those include files everything should be initialise

#

maybe an exorcisme of the machine 👀 hi! hi!

broken jay
#

Bed mesh min Y origin value was -7.0 giving move out of range on Y
min_Mesh_Y = 20 beacon_Y_offset= 27 20-27= -7.0

setting my min mesh Y at 30 fixed the problem
[bed_mesh]
mesh_min: 20,30

from RatOS/printers/v-core-3/300.cfg
[bed_mesh]
mesh_min: 20,20

from RatOS/z-probe/beacon.cfg
[beacon]
x_offset: 0
y_offset: 27

from klippy.log
bed_mesh: generated points
Index | Tool Adjusted | Probe
0 | (20.0, -7.0) | (20.0, 20.0)
1 | (60.8, -7.0) | (60.8, 20.0)
2 | (101.7, -7.0) | (101.7, 20.0)
3 | (142.5, -7.0) | (142.5, 20.0)
4 | (183.3, -7.0) | (183.3, 20.0)
5 | (224.1, -7.0) | (224.1, 20.0)
6 | (265.0, -7.0) | (265.0, 20.0)
7 | (265.0, 33.0) | (265.0, 60.0)
8 | (224.2, 33.0) | (224.2, 60.0)
9 | (183.3, 33.0) | (183.3, 60.0)
10 | (142.5, 33.0) | (142.5, 60.0)
...

fast elk
#

sure, because, 30 minus 27 is positive. If you do a bed mesh now you might see a funny bed mesh. Taht is because the eaddy current isn´t laser like. Better to move it 40 away from the borders of the bed.

broken jay
#

👍

soft sun
#

Something I changed in my config is the points of probing with beacon for Tilte. Because the X offset is zero, i changed the rear probing point of the lead screw to half the size of my printer so in your case should be 150,270