Running into an issue with my fresh 2.4 build. Using base config off GitHub for the octopus Pro with minor tweaks for EBB36 and my set up. Machine homes X and Y with no issue, Z moves maybe 10mm down and faults out and throws out “No trigger on Z after full movement”
Anyone run into this before?
Specs:
V2.4 350mm self source
XOL tool head with Sherpa mini and Rapido HF controlled by a EBB36 V1.2 and U2C
BTT MicroProbe v1.2
LDO Motor Kit
Octopus Pro v1.0.1
Pi 3B
BFI - BZI
Pin Mod
GE5C Z mod