#No trigger on Z after full movement

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storm nacelle
#

Running into an issue with my fresh 2.4 build. Using base config off GitHub for the octopus Pro with minor tweaks for EBB36 and my set up. Machine homes X and Y with no issue, Z moves maybe 10mm down and faults out and throws out “No trigger on Z after full movement”

Anyone run into this before?

Specs:
V2.4 350mm self source
XOL tool head with Sherpa mini and Rapido HF controlled by a EBB36 V1.2 and U2C
BTT MicroProbe v1.2
LDO Motor Kit
Octopus Pro v1.0.1
Pi 3B
BFI - BZI
Pin Mod
GE5C Z mod

jagged garden
#

This error happens when your printer's z axis has travelled (z_max-z_min) while homing, without registering that the z_home switch has been hit.

what are your Z_max and Z_min values?

storm nacelle
#

Z max was set 350 and Z min -10, I’ve tried changing these values without any change in results